summaryrefslogtreecommitdiff
diff options
context:
space:
mode:
authorDuncan Laurie <dlaurie@chromium.org>2013-05-13 10:08:22 -0700
committerChromeBot <chrome-bot@google.com>2013-05-13 19:31:11 -0700
commitc18ef5f4219fddf36052abb5052396808c4fca4a (patch)
treee8ba171a1bec246f6a93a5b386d8fb9f68c69d54
parent59921512e7c634532827df016c54ea5932de4e1f (diff)
downloadchrome-ec-c18ef5f4219fddf36052abb5052396808c4fca4a.tar.gz
slippy: Enable internal pullup for recovery pin
The recovery pin input from servo is open drain and needs an internal pullup enabled so it is not always low. BUG=chrome-os-partner:19398 BRANCH=none TEST=manual: ensure rec_mode can be turned off $ dut-control rec_mode:off rec_mode rec_mode:off Change-Id: I387a53eb5b64bb0bf3a87fc47b5cca9b2063f6a9 Signed-off-by: Duncan Laurie <dlaurie@chromium.org> Reviewed-on: https://gerrit.chromium.org/gerrit/50993
-rw-r--r--board/slippy/board.c2
1 files changed, 1 insertions, 1 deletions
diff --git a/board/slippy/board.c b/board/slippy/board.c
index d49b95c72b..c1cbdb79a6 100644
--- a/board/slippy/board.c
+++ b/board/slippy/board.c
@@ -55,7 +55,7 @@ const struct gpio_info gpio_list[GPIO_COUNT] = {
x86_power_interrupt},
{"PCH_EDP_VDD_EN", LM4_GPIO_J, (1<<1), GPIO_INT_BOTH,
x86_power_interrupt},
- {"RECOVERY_L", LM4_GPIO_A, (1<<5), GPIO_INT_BOTH,
+ {"RECOVERY_L", LM4_GPIO_A, (1<<5), GPIO_PULL_UP|GPIO_INT_BOTH,
switch_interrupt},
{"WRITE_PROTECT", LM4_GPIO_A, (1<<4), GPIO_INT_BOTH,
switch_interrupt},