summaryrefslogtreecommitdiff
path: root/board
diff options
context:
space:
mode:
authorNicolas Boichat <drinkcat@google.com>2017-03-08 11:24:53 -0800
committerchrome-bot <chrome-bot@chromium.org>2017-03-10 15:11:56 -0800
commit2a149154c4e5d06aa9fc3a007cca05890e09e583 (patch)
tree7a690af009377bf5b9791bcf4365bda39c470c48 /board
parent7277708e43195e8ea4d83c649de2d8c4a144b90a (diff)
downloadchrome-ec-2a149154c4e5d06aa9fc3a007cca05890e09e583.tar.gz
hammer: Enable internal pull-up on UART RX line
Prevent spurious wake when servo is not connected. BRANCH=none BUG=b:36119938 TEST=Measure pull up value with a multimeter when servo is not connected: value around 30k when host in S0 and S3. Change-Id: I8bd54e4dcfd5c65f1f0cd32ffd4a70cedb979cc2 Reviewed-on: https://chromium-review.googlesource.com/452652 Commit-Ready: Nicolas Boichat <drinkcat@chromium.org> Tested-by: Nicolas Boichat <drinkcat@chromium.org> Reviewed-by: Vincent Palatin <vpalatin@chromium.org>
Diffstat (limited to 'board')
-rw-r--r--board/hammer/gpio.inc2
1 files changed, 1 insertions, 1 deletions
diff --git a/board/hammer/gpio.inc b/board/hammer/gpio.inc
index bc8dbdfd0b..6ab26af4ec 100644
--- a/board/hammer/gpio.inc
+++ b/board/hammer/gpio.inc
@@ -52,7 +52,7 @@ GPIO(WP_L, PIN(A, 13), GPIO_INPUT)
/* Unimplemented signals since we are not an EC */
UNIMPLEMENTED(ENTERING_RW)
-ALTERNATE(PIN_MASK(A, 0x0600), 1, MODULE_UART, 0) /* USART1: PA09/PA10 - Servo stm32 console UART */
+ALTERNATE(PIN_MASK(A, 0x0600), 1, MODULE_UART, GPIO_PULL_UP) /* USART1: PA09/PA10 - Servo stm32 console UART */
ALTERNATE(PIN_MASK(B, 0x00c0), 1, MODULE_I2C, 0) /* I2C MASTER:PB6/7 GPIO_ODR_HIGH */