diff options
author | Aaron Durbin <adurbin@chromium.org> | 2013-05-22 12:41:08 -0500 |
---|---|---|
committer | ChromeBot <chrome-bot@google.com> | 2013-05-22 12:29:11 -0700 |
commit | 3ca68b3134ae53f707a464458060d45f0a8a9ce4 (patch) | |
tree | e7877a66ba29a6e6b79747e48d838843bd176526 /board | |
parent | 93ec62ebc3ae238749915f8161a2673a7d2928d9 (diff) | |
download | chrome-ec-3ca68b3134ae53f707a464458060d45f0a8a9ce4.tar.gz |
haswell: fix RCIN# GPIO setting
The gpio pin used for RCIN# should be configured as open drain as the
rail is pulled up by a non-EC rail. Driving it high would leak power.
The current GPIO_HI_Z macro uses GPIO_HIGH as the default state.
However, it has been found that this actually drives the pin to ground.
It is still unclear how Link works or doesn't.
BUG=chrome-os-partner:19355
BRANCH=none
TEST=manual: boot on slippy without RCIN# causing reset and
the 'apreset warm' EC command works as expected.
Change-Id: I71425075f8d77b3d7e576a59fc24f823790e2655
Signed-off-by: Aaron Durbin <adurbin@chromium.org>
Reviewed-on: https://gerrit.chromium.org/gerrit/56269
Reviewed-by: Duncan Laurie <dlaurie@chromium.org>
Diffstat (limited to 'board')
-rw-r--r-- | board/slippy/board.c | 2 |
1 files changed, 1 insertions, 1 deletions
diff --git a/board/slippy/board.c b/board/slippy/board.c index 5fe222ff33..55f1d4a8d8 100644 --- a/board/slippy/board.c +++ b/board/slippy/board.c @@ -95,7 +95,7 @@ const struct gpio_info gpio_list[GPIO_COUNT] = { {"PCH_NMI_L", LM4_GPIO_F, (1<<2), GPIO_OUT_HIGH, NULL}, {"PCH_PWRBTN_L", LM4_GPIO_H, (1<<0), GPIO_OUT_HIGH, NULL}, {"PCH_PWROK", LM4_GPIO_F, (1<<5), GPIO_OUT_LOW, NULL}, - {"PCH_RCIN_L", LM4_GPIO_L, (1<<6), GPIO_OUT_HIGH, NULL}, + {"PCH_RCIN_L", LM4_GPIO_L, (1<<6), GPIO_HI_Z_OPEN, NULL}, {"PCH_RSMRST_L", LM4_GPIO_F, (1<<1), GPIO_OUT_LOW, NULL}, {"PCH_SMI_L", LM4_GPIO_F, (1<<4), GPIO_OUT_HIGH, NULL}, {"TOUCHSCREEN_RESET_L", LM4_GPIO_N, (1<<7), GPIO_OUT_LOW, NULL}, |